A pilot-scale upflow anaerobic sludge blanket (UASB)-downflow hanging sponge system (DHS) combined with an anaerobic baffled reactor (ABR) and a settling tank (ST) was installed in a natural rubber processing… Click to show full abstract
A pilot-scale upflow anaerobic sludge blanket (UASB)-downflow hanging sponge system (DHS) combined with an anaerobic baffled reactor (ABR) and a settling tank (ST) was installed in a natural rubber processing factory in South Vietnam and its process performance was evaluated for 267days. The UASB reactor achieved a total removal efficiency of 55.6±16.6% for chemical oxygen demand (COD) and 77.8±10.3% for biochemical oxygen demand (BOD) with an organic loading rate of 1.7±0.6kg-COD·m-3·day-1. The final effluent of the proposed system had 140±64mg·L-1 of total COD, 31±12mg·L-1 of total BOD, and 58±24mg-N·L-1 of total nitrogen. The system could significantly reduce 92% of greenhouse gas emissions and 80% of hydraulic retention times compared with current treatment systems.
               
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