Purified terephthalic acid (PTA) wastewater with properties of poor biodegradation and high toxicity is produced from refining and synthesis of petrochemical products. In this study, a lab-scale hollow fiber membrane… Click to show full abstract
Purified terephthalic acid (PTA) wastewater with properties of poor biodegradation and high toxicity is produced from refining and synthesis of petrochemical products. In this study, a lab-scale hollow fiber membrane bioreactor (HF-AnMBR) fed with synthetic PTA wastewater was operated over 200 days with stepwise decreased hydraulic retention time (HRT) to investigate the long-term performance, membrane fouling mechanism and microbial community evolution. Results showed that a stable chemical oxygen demand (COD) removal rate of 65.8 ± 4.1% was achieved at organic loading rate of 3.1 ± 0.3 g-COD/L-reactor/d and HRT 24 h, under which the methane production rate reached 0.33 ± 0.02 L/L-reactor/d. Further shortening HRT, however, led to the decreased COD removal efficiency and low methane bioconversion. A mild membrane fouling occurred due to the production of colloidal biopolymers and the interaction between increased colloidal substances secreted/cracked by microorganisms and membrane interface. Further 16S rRNA analysis indicated that microbial diversity and richness had changed with the variation of HRT while Methanosaeta, and Methanolinea species were always the dominant methanogens responsible for methane production. The results verify that HF-AnMBR is an alternative technology for PTA wastewater treatment along with energy harvesting, and provide a new avenue toward sustainable petrochemical wastewater management.
               
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